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This research discusses the case study of optimization of rocket RWX 200 motor tube with carbon fiber reinforced for 2 through 6 mm thickness. Carbon fiber is chosen due to its mechanical properties such as high strength and stiffness, and high temperature resistance, as the specification needs of t...

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Main Author: GUNAWAN PUTRA (NIM : 23607302); Pembimbing : Dr. Ir. Bambang Kismono Hadi, RONALD
Format: Theses
Language:Indonesia
Online Access:https://digilib.itb.ac.id/gdl/view/17080
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Institution: Institut Teknologi Bandung
Language: Indonesia
id id-itb.:17080
spelling id-itb.:170802017-10-09T10:19:32Z#TITLE_ALTERNATIVE# GUNAWAN PUTRA (NIM : 23607302); Pembimbing : Dr. Ir. Bambang Kismono Hadi, RONALD Indonesia Theses INSTITUT TEKNOLOGI BANDUNG https://digilib.itb.ac.id/gdl/view/17080 This research discusses the case study of optimization of rocket RWX 200 motor tube with carbon fiber reinforced for 2 through 6 mm thickness. Carbon fiber is chosen due to its mechanical properties such as high strength and stiffness, and high temperature resistance, as the specification needs of the rocket motor tube. Rocket motor tube is made from weaving method, while the analysis and simulation is done by assuming it as laminate with the [0/90]s stacking sequence. <br /> <br /> <br /> <br /> From the calculation and simulation, it is determined that the X stress component of the laminates is below the strength of the material, while the Y stress component is beyond the strength of the material. It can be concluded that 900 laminae in each laminates has been failed. text
institution Institut Teknologi Bandung
building Institut Teknologi Bandung Library
continent Asia
country Indonesia
Indonesia
content_provider Institut Teknologi Bandung
collection Digital ITB
language Indonesia
description This research discusses the case study of optimization of rocket RWX 200 motor tube with carbon fiber reinforced for 2 through 6 mm thickness. Carbon fiber is chosen due to its mechanical properties such as high strength and stiffness, and high temperature resistance, as the specification needs of the rocket motor tube. Rocket motor tube is made from weaving method, while the analysis and simulation is done by assuming it as laminate with the [0/90]s stacking sequence. <br /> <br /> <br /> <br /> From the calculation and simulation, it is determined that the X stress component of the laminates is below the strength of the material, while the Y stress component is beyond the strength of the material. It can be concluded that 900 laminae in each laminates has been failed.
format Theses
author GUNAWAN PUTRA (NIM : 23607302); Pembimbing : Dr. Ir. Bambang Kismono Hadi, RONALD
spellingShingle GUNAWAN PUTRA (NIM : 23607302); Pembimbing : Dr. Ir. Bambang Kismono Hadi, RONALD
#TITLE_ALTERNATIVE#
author_facet GUNAWAN PUTRA (NIM : 23607302); Pembimbing : Dr. Ir. Bambang Kismono Hadi, RONALD
author_sort GUNAWAN PUTRA (NIM : 23607302); Pembimbing : Dr. Ir. Bambang Kismono Hadi, RONALD
title #TITLE_ALTERNATIVE#
title_short #TITLE_ALTERNATIVE#
title_full #TITLE_ALTERNATIVE#
title_fullStr #TITLE_ALTERNATIVE#
title_full_unstemmed #TITLE_ALTERNATIVE#
title_sort #title_alternative#
url https://digilib.itb.ac.id/gdl/view/17080
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