Failure Analysis of TJ-24 Turbojet Through Literature and Experimental Study

<p align="justify"> The ability to develop micro turbojet is important for a country, especially Indonesia, because of its wide range application and crucial role. In ITB Mechanical Engineering Department, a micro turbojet with 24 Newton thrust specification was being developed under...

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Main Author: RIZKY LAKSANA (nim : 13114056), AKBAR
Format: Final Project
Language:Indonesia
Online Access:https://digilib.itb.ac.id/gdl/view/25266
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Institution: Institut Teknologi Bandung
Language: Indonesia
id id-itb.:25266
spelling id-itb.:252662018-07-02T07:27:48ZFailure Analysis of TJ-24 Turbojet Through Literature and Experimental Study RIZKY LAKSANA (nim : 13114056), AKBAR Indonesia Final Project INSTITUT TEKNOLOGI BANDUNG https://digilib.itb.ac.id/gdl/view/25266 <p align="justify"> The ability to develop micro turbojet is important for a country, especially Indonesia, because of its wide range application and crucial role. In ITB Mechanical Engineering Department, a micro turbojet with 24 Newton thrust specification was being developed under the name of TJ-24 from 2006 until now. Until now, TJ-24 has not yet able to reach idle operation and generate thrust force. TJ-24’s condition in the beginning of this project was unable to operate due to damage to the fuel pipe, NGV, and turbine components in previous research that generated 0.981 N thrust at 13,000 rpm. <br /> <br /> Reparation and replacement on the components stated above the were done to restore TJ-24’s conditions back to operable conditions and to conduct further testing. Testing is intended to measure compressor outlet pressure, compressor outlet temperature, turbine inlet temperature, turbine outlet temperature, fuel flow, also rotation and thrust force. <br /> <br /> Testing results shows that the maximum temperature reached was only 330 oC, the flame position was downstream of combustion chamber, compressor could not deliver pressure rise, and fuel flow only reached 23-28 g/min. Rotation speed only reached 5,400 rpm and no thrust were generated. Testing results yields a failure cause; diffusor is not optimal, combustion chamber design and geometry is not optimal, casing deformation, and absence of lubrication. <br /> <p align="justify"> text
institution Institut Teknologi Bandung
building Institut Teknologi Bandung Library
continent Asia
country Indonesia
Indonesia
content_provider Institut Teknologi Bandung
collection Digital ITB
language Indonesia
description <p align="justify"> The ability to develop micro turbojet is important for a country, especially Indonesia, because of its wide range application and crucial role. In ITB Mechanical Engineering Department, a micro turbojet with 24 Newton thrust specification was being developed under the name of TJ-24 from 2006 until now. Until now, TJ-24 has not yet able to reach idle operation and generate thrust force. TJ-24’s condition in the beginning of this project was unable to operate due to damage to the fuel pipe, NGV, and turbine components in previous research that generated 0.981 N thrust at 13,000 rpm. <br /> <br /> Reparation and replacement on the components stated above the were done to restore TJ-24’s conditions back to operable conditions and to conduct further testing. Testing is intended to measure compressor outlet pressure, compressor outlet temperature, turbine inlet temperature, turbine outlet temperature, fuel flow, also rotation and thrust force. <br /> <br /> Testing results shows that the maximum temperature reached was only 330 oC, the flame position was downstream of combustion chamber, compressor could not deliver pressure rise, and fuel flow only reached 23-28 g/min. Rotation speed only reached 5,400 rpm and no thrust were generated. Testing results yields a failure cause; diffusor is not optimal, combustion chamber design and geometry is not optimal, casing deformation, and absence of lubrication. <br /> <p align="justify">
format Final Project
author RIZKY LAKSANA (nim : 13114056), AKBAR
spellingShingle RIZKY LAKSANA (nim : 13114056), AKBAR
Failure Analysis of TJ-24 Turbojet Through Literature and Experimental Study
author_facet RIZKY LAKSANA (nim : 13114056), AKBAR
author_sort RIZKY LAKSANA (nim : 13114056), AKBAR
title Failure Analysis of TJ-24 Turbojet Through Literature and Experimental Study
title_short Failure Analysis of TJ-24 Turbojet Through Literature and Experimental Study
title_full Failure Analysis of TJ-24 Turbojet Through Literature and Experimental Study
title_fullStr Failure Analysis of TJ-24 Turbojet Through Literature and Experimental Study
title_full_unstemmed Failure Analysis of TJ-24 Turbojet Through Literature and Experimental Study
title_sort failure analysis of tj-24 turbojet through literature and experimental study
url https://digilib.itb.ac.id/gdl/view/25266
_version_ 1821910376306966528