PERBAIKAN KUALITAS STASIUN KERJA MESIN BUBUT PADA PT. DIRGANTARA INDONESIA DENGAN METODE SIX SIGMA

PT Digantara Indonesia (DI) has a division, in charge of making aerospace parts regularly, namely detail parts manufactuing (DPM). Based on PT DI’s data, reject rate of DPM in last 3 years were above the target, which is 0,5%. Therefore, further experiment should be conducted on the area that contri...

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Main Author: Nadira Ramadhani, Nisa
Format: Final Project
Language:Indonesia
Online Access:https://digilib.itb.ac.id/gdl/view/53977
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Institution: Institut Teknologi Bandung
Language: Indonesia
id id-itb.:53977
spelling id-itb.:539772021-03-12T14:50:48ZPERBAIKAN KUALITAS STASIUN KERJA MESIN BUBUT PADA PT. DIRGANTARA INDONESIA DENGAN METODE SIX SIGMA Nadira Ramadhani, Nisa Indonesia Final Project six sigma, lathe machine, define, measure, analyze, improve, and control. INSTITUT TEKNOLOGI BANDUNG https://digilib.itb.ac.id/gdl/view/53977 PT Digantara Indonesia (DI) has a division, in charge of making aerospace parts regularly, namely detail parts manufactuing (DPM). Based on PT DI’s data, reject rate of DPM in last 3 years were above the target, which is 0,5%. Therefore, further experiment should be conducted on the area that contributed to the reject area, such as lathe machine. This experiment recommend six sigma method with DMAIC approach (Define, Measure, Analyze, Improve, Control) to elaborate on improvements in lathe machine area. In the define step, types of defects were determined. In the measure step, process stability was determined with control chart and process capability was calculated. In analyze step, root causes were determined with the usage of cause & effect diagrams and 5 whys, and FMEA (Failure Mode Effect & Analysis). In improve step, recommendation solutions from determined root causes are determined. In control step, recommendation for hold in the solution was made The type of defects that needed to be solved are undersize and damaged. Then, the result of measure step were lathe machine process is in stable condition and the result of process capability was 3,38 sigma. Then, from the result of analysis, root causes are determined. There are 1) cutting condition table had not been created, 2) other measuring tools comparison had not been created, 3) method for checking cutting tools before using it had not been created, 4) guide of machine usage for operator had not been made, and 5) standard method of setting & media for checking after setting had not been made. Then, the solution for those root causes are 1) making a cutting condition usage table, 2) making a measuring tool usage table, and 3) a standard operating procedure (SOP) of lathe machine. text
institution Institut Teknologi Bandung
building Institut Teknologi Bandung Library
continent Asia
country Indonesia
Indonesia
content_provider Institut Teknologi Bandung
collection Digital ITB
language Indonesia
description PT Digantara Indonesia (DI) has a division, in charge of making aerospace parts regularly, namely detail parts manufactuing (DPM). Based on PT DI’s data, reject rate of DPM in last 3 years were above the target, which is 0,5%. Therefore, further experiment should be conducted on the area that contributed to the reject area, such as lathe machine. This experiment recommend six sigma method with DMAIC approach (Define, Measure, Analyze, Improve, Control) to elaborate on improvements in lathe machine area. In the define step, types of defects were determined. In the measure step, process stability was determined with control chart and process capability was calculated. In analyze step, root causes were determined with the usage of cause & effect diagrams and 5 whys, and FMEA (Failure Mode Effect & Analysis). In improve step, recommendation solutions from determined root causes are determined. In control step, recommendation for hold in the solution was made The type of defects that needed to be solved are undersize and damaged. Then, the result of measure step were lathe machine process is in stable condition and the result of process capability was 3,38 sigma. Then, from the result of analysis, root causes are determined. There are 1) cutting condition table had not been created, 2) other measuring tools comparison had not been created, 3) method for checking cutting tools before using it had not been created, 4) guide of machine usage for operator had not been made, and 5) standard method of setting & media for checking after setting had not been made. Then, the solution for those root causes are 1) making a cutting condition usage table, 2) making a measuring tool usage table, and 3) a standard operating procedure (SOP) of lathe machine.
format Final Project
author Nadira Ramadhani, Nisa
spellingShingle Nadira Ramadhani, Nisa
PERBAIKAN KUALITAS STASIUN KERJA MESIN BUBUT PADA PT. DIRGANTARA INDONESIA DENGAN METODE SIX SIGMA
author_facet Nadira Ramadhani, Nisa
author_sort Nadira Ramadhani, Nisa
title PERBAIKAN KUALITAS STASIUN KERJA MESIN BUBUT PADA PT. DIRGANTARA INDONESIA DENGAN METODE SIX SIGMA
title_short PERBAIKAN KUALITAS STASIUN KERJA MESIN BUBUT PADA PT. DIRGANTARA INDONESIA DENGAN METODE SIX SIGMA
title_full PERBAIKAN KUALITAS STASIUN KERJA MESIN BUBUT PADA PT. DIRGANTARA INDONESIA DENGAN METODE SIX SIGMA
title_fullStr PERBAIKAN KUALITAS STASIUN KERJA MESIN BUBUT PADA PT. DIRGANTARA INDONESIA DENGAN METODE SIX SIGMA
title_full_unstemmed PERBAIKAN KUALITAS STASIUN KERJA MESIN BUBUT PADA PT. DIRGANTARA INDONESIA DENGAN METODE SIX SIGMA
title_sort perbaikan kualitas stasiun kerja mesin bubut pada pt. dirgantara indonesia dengan metode six sigma
url https://digilib.itb.ac.id/gdl/view/53977
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