PROCESS OPTIMATION AT CONDENSATE STRIPPER REBOILER TO REDUCE ETHANE CONTENT AT NGL PRODUCT AND REDUCE FLARED GAS AT FIXED PRODUCTION UNIT FOR PROPANE LPG PRODUCTION

ABSTRACT PROCESS OPTIMATION AT CONDENSATE STRIPPER REBOILER TO REDUCE ETHANE CONTENT AT NGL PRODUCT AND REDUCE FLARED GAS AT FIXED PRODUCTION UNIT FOR PROPANE LPG PRODUCTION oleh Ekawati NIM : 23015021 (Master’s Program in Chemical Engineering) A multinational gas company operating at Sumatra...

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Main Author: Ekawati
Format: Theses
Language:Indonesia
Online Access:https://digilib.itb.ac.id/gdl/view/54678
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Institution: Institut Teknologi Bandung
Language: Indonesia
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spelling id-itb.:546782021-05-05T10:08:42ZPROCESS OPTIMATION AT CONDENSATE STRIPPER REBOILER TO REDUCE ETHANE CONTENT AT NGL PRODUCT AND REDUCE FLARED GAS AT FIXED PRODUCTION UNIT FOR PROPANE LPG PRODUCTION Ekawati Indonesia Theses NGL Production Optimization, Emission Reduction on Flared Gas, Optimization of Condensate Stripper Operation INSTITUT TEKNOLOGI BANDUNG https://digilib.itb.ac.id/gdl/view/54678 ABSTRACT PROCESS OPTIMATION AT CONDENSATE STRIPPER REBOILER TO REDUCE ETHANE CONTENT AT NGL PRODUCT AND REDUCE FLARED GAS AT FIXED PRODUCTION UNIT FOR PROPANE LPG PRODUCTION oleh Ekawati NIM : 23015021 (Master’s Program in Chemical Engineering) A multinational gas company operating at Sumatra Island is processing 260 MMscfd of natural gas to produce around 110 MMscfd of gas sales and 26,000 bpd of NGL products. The purpose of this study is to optimize the operation in order the C2 / C3 ratio of NGL products does not exceed 2.0%, in accordance with the technical specifications required for NGL products. Prior to optimization, the C2 / C3 ratio of NGL products was 4.95%. The constraints to be considered in optimization are the maximum gas flow rate of 260 MMscfd to LP Inlet Compressor (K-201A / B / C), maximum gas flow rate of 177 MMscfd on CO2 removal unit, maximum 37,0% CO2 content at CO2 removal, and pressure on the Condensate Stripper column does not exceed 270 psig. Optimization is done by changing the operating pressure on Condensate Stripper column (C-201), temperature on Pretreament Chiller (E-103) and temperature on Condensate Stripper Reboiler (E-106). Optimization results showed that optimum conditions were achieved when the operating pressure on the Condensate Stripper column (C-201) was changed from 250 psig to 267 psig, the temperature at Pretreatment Chiller (E-103) changed from 65oF to 70oF and Condensate Stripper Reboiler (E-106) changed from 245oF to 267oF with these optimum condition, the C2 / C3 ratio of NGL products has been reduced to 1.38% (simulation), 2.0% (actual). Process optimization has been succeeded in lowering the flared gas in Fixed Platform Unit from 5 MMscfd to not exceed 1 MMscfd. text
institution Institut Teknologi Bandung
building Institut Teknologi Bandung Library
continent Asia
country Indonesia
Indonesia
content_provider Institut Teknologi Bandung
collection Digital ITB
language Indonesia
description ABSTRACT PROCESS OPTIMATION AT CONDENSATE STRIPPER REBOILER TO REDUCE ETHANE CONTENT AT NGL PRODUCT AND REDUCE FLARED GAS AT FIXED PRODUCTION UNIT FOR PROPANE LPG PRODUCTION oleh Ekawati NIM : 23015021 (Master’s Program in Chemical Engineering) A multinational gas company operating at Sumatra Island is processing 260 MMscfd of natural gas to produce around 110 MMscfd of gas sales and 26,000 bpd of NGL products. The purpose of this study is to optimize the operation in order the C2 / C3 ratio of NGL products does not exceed 2.0%, in accordance with the technical specifications required for NGL products. Prior to optimization, the C2 / C3 ratio of NGL products was 4.95%. The constraints to be considered in optimization are the maximum gas flow rate of 260 MMscfd to LP Inlet Compressor (K-201A / B / C), maximum gas flow rate of 177 MMscfd on CO2 removal unit, maximum 37,0% CO2 content at CO2 removal, and pressure on the Condensate Stripper column does not exceed 270 psig. Optimization is done by changing the operating pressure on Condensate Stripper column (C-201), temperature on Pretreament Chiller (E-103) and temperature on Condensate Stripper Reboiler (E-106). Optimization results showed that optimum conditions were achieved when the operating pressure on the Condensate Stripper column (C-201) was changed from 250 psig to 267 psig, the temperature at Pretreatment Chiller (E-103) changed from 65oF to 70oF and Condensate Stripper Reboiler (E-106) changed from 245oF to 267oF with these optimum condition, the C2 / C3 ratio of NGL products has been reduced to 1.38% (simulation), 2.0% (actual). Process optimization has been succeeded in lowering the flared gas in Fixed Platform Unit from 5 MMscfd to not exceed 1 MMscfd.
format Theses
author Ekawati
spellingShingle Ekawati
PROCESS OPTIMATION AT CONDENSATE STRIPPER REBOILER TO REDUCE ETHANE CONTENT AT NGL PRODUCT AND REDUCE FLARED GAS AT FIXED PRODUCTION UNIT FOR PROPANE LPG PRODUCTION
author_facet Ekawati
author_sort Ekawati
title PROCESS OPTIMATION AT CONDENSATE STRIPPER REBOILER TO REDUCE ETHANE CONTENT AT NGL PRODUCT AND REDUCE FLARED GAS AT FIXED PRODUCTION UNIT FOR PROPANE LPG PRODUCTION
title_short PROCESS OPTIMATION AT CONDENSATE STRIPPER REBOILER TO REDUCE ETHANE CONTENT AT NGL PRODUCT AND REDUCE FLARED GAS AT FIXED PRODUCTION UNIT FOR PROPANE LPG PRODUCTION
title_full PROCESS OPTIMATION AT CONDENSATE STRIPPER REBOILER TO REDUCE ETHANE CONTENT AT NGL PRODUCT AND REDUCE FLARED GAS AT FIXED PRODUCTION UNIT FOR PROPANE LPG PRODUCTION
title_fullStr PROCESS OPTIMATION AT CONDENSATE STRIPPER REBOILER TO REDUCE ETHANE CONTENT AT NGL PRODUCT AND REDUCE FLARED GAS AT FIXED PRODUCTION UNIT FOR PROPANE LPG PRODUCTION
title_full_unstemmed PROCESS OPTIMATION AT CONDENSATE STRIPPER REBOILER TO REDUCE ETHANE CONTENT AT NGL PRODUCT AND REDUCE FLARED GAS AT FIXED PRODUCTION UNIT FOR PROPANE LPG PRODUCTION
title_sort process optimation at condensate stripper reboiler to reduce ethane content at ngl product and reduce flared gas at fixed production unit for propane lpg production
url https://digilib.itb.ac.id/gdl/view/54678
_version_ 1822001847974494208