STUDI DE-BOTTLENECKING LAPANGAN MINYAK X UNTUK MENGEVALUASI PENINGKATAN PRODUKTIVITAS MELALUI PENGURANGAN TEKANAN SISTEM DENGAN INSTALASI BOOSTER PUMP

X Area is a field owned by one of Oil and Gas Company in Indonesia which is operating as a contractor with Production Sharing Contract deal with the Indonesian Government. Currently X Area has 14 offshore platforms which consist of 63 production wells and one process platform. The entire production...

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Main Author: Taufan, Muhammad
Format: Final Project
Language:Indonesia
Subjects:
Online Access:https://digilib.itb.ac.id/gdl/view/60958
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Institution: Institut Teknologi Bandung
Language: Indonesia
id id-itb.:60958
spelling id-itb.:609582021-09-21T16:30:13ZSTUDI DE-BOTTLENECKING LAPANGAN MINYAK X UNTUK MENGEVALUASI PENINGKATAN PRODUKTIVITAS MELALUI PENGURANGAN TEKANAN SISTEM DENGAN INSTALASI BOOSTER PUMP Taufan, Muhammad Pertambangan dan operasi berkaitan Indonesia Final Project De-Bottlenecking, Electric Submersible Pump, Booster Pump INSTITUT TEKNOLOGI BANDUNG https://digilib.itb.ac.id/gdl/view/60958 X Area is a field owned by one of Oil and Gas Company in Indonesia which is operating as a contractor with Production Sharing Contract deal with the Indonesian Government. Currently X Area has 14 offshore platforms which consist of 63 production wells and one process platform. The entire production wells are using Electric Submersible Pump (ESP). In the course of production process and pressure drop in the bottom hole pressure , dissolved gas in oil will separate into casing annulus which causes increasing casing pressure causing several issues including, bottlenecking phenomenon resulting from the casing pressure exceeds the riser pressure and decreasing fluid level. The problem becomes more complicated when all the wells merged into one integrated system, several wells were decreasing their productivity or even the production were shut down. The objective of this paper is to estimate the optimum operating system pressure and evaluate productivity improvement through system pressure reduction by installing booster pump. The evaluation methods used include modeling and simulation (matching) wells and the results used to develop subsea pipeline network model and simulation using commercial simulator. After getting matching results, optimization scenarios performed including the addition of booster pump. The results of this study showed an increase 50.8% in productivity compared to the actual conditions text
institution Institut Teknologi Bandung
building Institut Teknologi Bandung Library
continent Asia
country Indonesia
Indonesia
content_provider Institut Teknologi Bandung
collection Digital ITB
language Indonesia
topic Pertambangan dan operasi berkaitan
spellingShingle Pertambangan dan operasi berkaitan
Taufan, Muhammad
STUDI DE-BOTTLENECKING LAPANGAN MINYAK X UNTUK MENGEVALUASI PENINGKATAN PRODUKTIVITAS MELALUI PENGURANGAN TEKANAN SISTEM DENGAN INSTALASI BOOSTER PUMP
description X Area is a field owned by one of Oil and Gas Company in Indonesia which is operating as a contractor with Production Sharing Contract deal with the Indonesian Government. Currently X Area has 14 offshore platforms which consist of 63 production wells and one process platform. The entire production wells are using Electric Submersible Pump (ESP). In the course of production process and pressure drop in the bottom hole pressure , dissolved gas in oil will separate into casing annulus which causes increasing casing pressure causing several issues including, bottlenecking phenomenon resulting from the casing pressure exceeds the riser pressure and decreasing fluid level. The problem becomes more complicated when all the wells merged into one integrated system, several wells were decreasing their productivity or even the production were shut down. The objective of this paper is to estimate the optimum operating system pressure and evaluate productivity improvement through system pressure reduction by installing booster pump. The evaluation methods used include modeling and simulation (matching) wells and the results used to develop subsea pipeline network model and simulation using commercial simulator. After getting matching results, optimization scenarios performed including the addition of booster pump. The results of this study showed an increase 50.8% in productivity compared to the actual conditions
format Final Project
author Taufan, Muhammad
author_facet Taufan, Muhammad
author_sort Taufan, Muhammad
title STUDI DE-BOTTLENECKING LAPANGAN MINYAK X UNTUK MENGEVALUASI PENINGKATAN PRODUKTIVITAS MELALUI PENGURANGAN TEKANAN SISTEM DENGAN INSTALASI BOOSTER PUMP
title_short STUDI DE-BOTTLENECKING LAPANGAN MINYAK X UNTUK MENGEVALUASI PENINGKATAN PRODUKTIVITAS MELALUI PENGURANGAN TEKANAN SISTEM DENGAN INSTALASI BOOSTER PUMP
title_full STUDI DE-BOTTLENECKING LAPANGAN MINYAK X UNTUK MENGEVALUASI PENINGKATAN PRODUKTIVITAS MELALUI PENGURANGAN TEKANAN SISTEM DENGAN INSTALASI BOOSTER PUMP
title_fullStr STUDI DE-BOTTLENECKING LAPANGAN MINYAK X UNTUK MENGEVALUASI PENINGKATAN PRODUKTIVITAS MELALUI PENGURANGAN TEKANAN SISTEM DENGAN INSTALASI BOOSTER PUMP
title_full_unstemmed STUDI DE-BOTTLENECKING LAPANGAN MINYAK X UNTUK MENGEVALUASI PENINGKATAN PRODUKTIVITAS MELALUI PENGURANGAN TEKANAN SISTEM DENGAN INSTALASI BOOSTER PUMP
title_sort studi de-bottlenecking lapangan minyak x untuk mengevaluasi peningkatan produktivitas melalui pengurangan tekanan sistem dengan instalasi booster pump
url https://digilib.itb.ac.id/gdl/view/60958
_version_ 1822003710311530496