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Production decline happened as X geothermal field being produced commercially since 1983. Well production decline rate evaluation is performed in purpose of extending the field production time. The used method is well-known Arps empiric method. Each well production decline rate is calculated and ana...

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Main Author: ABDILLAH (NIM 12204015), MU'THI
Format: Final Project
Language:Indonesia
Online Access:https://digilib.itb.ac.id/gdl/view/8761
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Institution: Institut Teknologi Bandung
Language: Indonesia
id id-itb.:8761
spelling id-itb.:87612017-09-27T10:37:31Z#TITLE_ALTERNATIVE# ABDILLAH (NIM 12204015), MU'THI Indonesia Final Project INSTITUT TEKNOLOGI BANDUNG https://digilib.itb.ac.id/gdl/view/8761 Production decline happened as X geothermal field being produced commercially since 1983. Well production decline rate evaluation is performed in purpose of extending the field production time. The used method is well-known Arps empiric method. Each well production decline rate is calculated and analyzed by how far re-injection programs affect production wells performance around injection well. The evaluation shows different production decline rate for each well in range 0.2-48.11 % /year and 7.09% /year average field production decline. Well 36, 37, and 38 give positive effect and so their operation can be still performed or considered. Well 39 and 40 give negative effect. Well 41 and 42 operations have to be reevaluated if there's appropriate data already. Low permeability area around well 5 and south well 4 can be considered as an injection area for south-east X Field site in supplying the new 60 MW unit. text
institution Institut Teknologi Bandung
building Institut Teknologi Bandung Library
continent Asia
country Indonesia
Indonesia
content_provider Institut Teknologi Bandung
collection Digital ITB
language Indonesia
description Production decline happened as X geothermal field being produced commercially since 1983. Well production decline rate evaluation is performed in purpose of extending the field production time. The used method is well-known Arps empiric method. Each well production decline rate is calculated and analyzed by how far re-injection programs affect production wells performance around injection well. The evaluation shows different production decline rate for each well in range 0.2-48.11 % /year and 7.09% /year average field production decline. Well 36, 37, and 38 give positive effect and so their operation can be still performed or considered. Well 39 and 40 give negative effect. Well 41 and 42 operations have to be reevaluated if there's appropriate data already. Low permeability area around well 5 and south well 4 can be considered as an injection area for south-east X Field site in supplying the new 60 MW unit.
format Final Project
author ABDILLAH (NIM 12204015), MU'THI
spellingShingle ABDILLAH (NIM 12204015), MU'THI
#TITLE_ALTERNATIVE#
author_facet ABDILLAH (NIM 12204015), MU'THI
author_sort ABDILLAH (NIM 12204015), MU'THI
title #TITLE_ALTERNATIVE#
title_short #TITLE_ALTERNATIVE#
title_full #TITLE_ALTERNATIVE#
title_fullStr #TITLE_ALTERNATIVE#
title_full_unstemmed #TITLE_ALTERNATIVE#
title_sort #title_alternative#
url https://digilib.itb.ac.id/gdl/view/8761
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