A detailed study of effects of row trenched holes at the combustor exit on film cooling effectiveness

The current research was performed in order to analyze the effects of cylindrical and row trench cooling holes with the alignment angle of 90 degrees on the film-cooling effectiveness near the combustor endwall surface at the blowing ratio of BR=3.18. The three-dimensional representation of a Pratt...

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Main Authors: Kianpour, Ehsan, Che Sidik, Nor Azwadi
Format: Article
Language:English
Published: Serbian Society of Computational Mechanics 2017
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Online Access:http://eprints.utm.my/id/eprint/77483/1/NorAzwadiCheSidik2017_ADetailedStudyofEffectsofRowTrenchedHoles.pdf
http://eprints.utm.my/id/eprint/77483/
http://dx.doi.org/10.24874/jsscm.2017.11.01.06
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Institution: Universiti Teknologi Malaysia
Language: English
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spelling my.utm.774832018-11-30T07:09:46Z http://eprints.utm.my/id/eprint/77483/ A detailed study of effects of row trenched holes at the combustor exit on film cooling effectiveness Kianpour, Ehsan Che Sidik, Nor Azwadi TC Hydraulic engineering. Ocean engineering The current research was performed in order to analyze the effects of cylindrical and row trench cooling holes with the alignment angle of 90 degrees on the film-cooling effectiveness near the combustor endwall surface at the blowing ratio of BR=3.18. The three-dimensional representation of a Pratt and Whitney gas turbine engine was simulated and analyzed with the commercial finite volume package, FLUENT 6.2.26. in order to find the most effective row trenched cooling holes. The analysis was done with Reynolds averaged Navier-Stokes turbulence model (RANS) on internal cooling passages. This combustor simulator was combined with the interaction of two rows of dilution jets, which were staggered in the stream-wise direction and aligned in the spanwise direction. In comparison with the baseline case of cooling holes, using a row trenched hole near the endwall surface increased the film-cooling effectiveness by 44% in average. Serbian Society of Computational Mechanics 2017 Article PeerReviewed application/pdf en http://eprints.utm.my/id/eprint/77483/1/NorAzwadiCheSidik2017_ADetailedStudyofEffectsofRowTrenchedHoles.pdf Kianpour, Ehsan and Che Sidik, Nor Azwadi (2017) A detailed study of effects of row trenched holes at the combustor exit on film cooling effectiveness. Journal of the Serbian Society for Computational Mechanics, 11 (1). pp. 59-68. ISSN 1820-6530 http://dx.doi.org/10.24874/jsscm.2017.11.01.06 DOI: 10.24874/jsscm.2017.11.01.06
institution Universiti Teknologi Malaysia
building UTM Library
collection Institutional Repository
continent Asia
country Malaysia
content_provider Universiti Teknologi Malaysia
content_source UTM Institutional Repository
url_provider http://eprints.utm.my/
language English
topic TC Hydraulic engineering. Ocean engineering
spellingShingle TC Hydraulic engineering. Ocean engineering
Kianpour, Ehsan
Che Sidik, Nor Azwadi
A detailed study of effects of row trenched holes at the combustor exit on film cooling effectiveness
description The current research was performed in order to analyze the effects of cylindrical and row trench cooling holes with the alignment angle of 90 degrees on the film-cooling effectiveness near the combustor endwall surface at the blowing ratio of BR=3.18. The three-dimensional representation of a Pratt and Whitney gas turbine engine was simulated and analyzed with the commercial finite volume package, FLUENT 6.2.26. in order to find the most effective row trenched cooling holes. The analysis was done with Reynolds averaged Navier-Stokes turbulence model (RANS) on internal cooling passages. This combustor simulator was combined with the interaction of two rows of dilution jets, which were staggered in the stream-wise direction and aligned in the spanwise direction. In comparison with the baseline case of cooling holes, using a row trenched hole near the endwall surface increased the film-cooling effectiveness by 44% in average.
format Article
author Kianpour, Ehsan
Che Sidik, Nor Azwadi
author_facet Kianpour, Ehsan
Che Sidik, Nor Azwadi
author_sort Kianpour, Ehsan
title A detailed study of effects of row trenched holes at the combustor exit on film cooling effectiveness
title_short A detailed study of effects of row trenched holes at the combustor exit on film cooling effectiveness
title_full A detailed study of effects of row trenched holes at the combustor exit on film cooling effectiveness
title_fullStr A detailed study of effects of row trenched holes at the combustor exit on film cooling effectiveness
title_full_unstemmed A detailed study of effects of row trenched holes at the combustor exit on film cooling effectiveness
title_sort detailed study of effects of row trenched holes at the combustor exit on film cooling effectiveness
publisher Serbian Society of Computational Mechanics
publishDate 2017
url http://eprints.utm.my/id/eprint/77483/1/NorAzwadiCheSidik2017_ADetailedStudyofEffectsofRowTrenchedHoles.pdf
http://eprints.utm.my/id/eprint/77483/
http://dx.doi.org/10.24874/jsscm.2017.11.01.06
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