A Systems study on the manufacturing system of Unilever Philippines' personal care plant

The study focused on the manufacturing system of Unilever Philippines' Personal Care Plant, which manufactures popular consumer brands such as Sunsilk, Vaseline, Ponds, Creamsilk, and others. After appraising the plant's present system, and evaluating, it turned out that the most prevalent...

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Main Authors: Li, Lindsey Darlene, Sy, Giza Eileene U.
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Language:English
Published: Animo Repository 2006
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Online Access:https://animorepository.dlsu.edu.ph/etd_bachelors/9397
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Institution: De La Salle University
Language: English
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spelling oai:animorepository.dlsu.edu.ph:etd_bachelors-100422021-09-06T23:56:25Z A Systems study on the manufacturing system of Unilever Philippines' personal care plant Li, Lindsey Darlene Sy, Giza Eileene U. The study focused on the manufacturing system of Unilever Philippines' Personal Care Plant, which manufactures popular consumer brands such as Sunsilk, Vaseline, Ponds, Creamsilk, and others. After appraising the plant's present system, and evaluating, it turned out that the most prevalent problem was that of the negative material variance that the plant has been experiencing. This led to the group's problem statement of: Unilever Philippine's Personal Care (PC) Plant has a material usage variance amounting to an actual loss of Php12.17 Million from October of 2004 to 2005 Analysis of the causes of material variance were presented and discussed in Chapter 5. It was identified that actual material variance led to three main factors: bulk adjustments (54%), rejects (22%) and wastes (18%). Although the study focused on solving actual material variance, solutions addressing system material variance were also presented. Alternative solutions were generated to address these specific problems and a proposed system was generated. For bulk adjustments, the group proposes a monthly calibration of the dosing machine. For bulk rejects, worker training and re-briefing and providing visual aids in the mixing area is proposed. Lastly, for wastes, the solution is to replace the Teflon diaphragm in the suction pump causing leftovers in the bestanks. Moreover, management has decided on which of group's generated alternative solutions is to be implement to address to the problem of system variance. These were: Reassign job functions for BPCS encoders, make new batch sheets with incorporated RM item codes, and provide BPCS manual to encoder for the problem on wrong and no encoding. In addition, assign a point person in the development to be in charge of BOM, make an amendment form, and implement a quarterly BOM review to address to the problem of not updated BOMs. Full implementation of the proposed solution is expected to reduce by a 79.50% in the total amount of actual material variance. Moreover, a minimum annual net savings of Php10.5 Million was computed with a net present value of Php42.88 Million in 5 years. 2006-01-01T08:00:00Z text https://animorepository.dlsu.edu.ph/etd_bachelors/9397 Bachelor's Theses English Animo Repository Unilever Philippines Manufacturing processes-- Philippines Production engineering--Philippines Production management--Philippines Hygiene products--Philippines Food processing plants-- Philippines Food processing by-products industry --Philippines Engineering
institution De La Salle University
building De La Salle University Library
continent Asia
country Philippines
Philippines
content_provider De La Salle University Library
collection DLSU Institutional Repository
language English
topic Unilever Philippines
Manufacturing processes-- Philippines
Production engineering--Philippines
Production management--Philippines
Hygiene products--Philippines
Food processing plants-- Philippines
Food processing by-products industry --Philippines
Engineering
spellingShingle Unilever Philippines
Manufacturing processes-- Philippines
Production engineering--Philippines
Production management--Philippines
Hygiene products--Philippines
Food processing plants-- Philippines
Food processing by-products industry --Philippines
Engineering
Li, Lindsey Darlene
Sy, Giza Eileene U.
A Systems study on the manufacturing system of Unilever Philippines' personal care plant
description The study focused on the manufacturing system of Unilever Philippines' Personal Care Plant, which manufactures popular consumer brands such as Sunsilk, Vaseline, Ponds, Creamsilk, and others. After appraising the plant's present system, and evaluating, it turned out that the most prevalent problem was that of the negative material variance that the plant has been experiencing. This led to the group's problem statement of: Unilever Philippine's Personal Care (PC) Plant has a material usage variance amounting to an actual loss of Php12.17 Million from October of 2004 to 2005 Analysis of the causes of material variance were presented and discussed in Chapter 5. It was identified that actual material variance led to three main factors: bulk adjustments (54%), rejects (22%) and wastes (18%). Although the study focused on solving actual material variance, solutions addressing system material variance were also presented. Alternative solutions were generated to address these specific problems and a proposed system was generated. For bulk adjustments, the group proposes a monthly calibration of the dosing machine. For bulk rejects, worker training and re-briefing and providing visual aids in the mixing area is proposed. Lastly, for wastes, the solution is to replace the Teflon diaphragm in the suction pump causing leftovers in the bestanks. Moreover, management has decided on which of group's generated alternative solutions is to be implement to address to the problem of system variance. These were: Reassign job functions for BPCS encoders, make new batch sheets with incorporated RM item codes, and provide BPCS manual to encoder for the problem on wrong and no encoding. In addition, assign a point person in the development to be in charge of BOM, make an amendment form, and implement a quarterly BOM review to address to the problem of not updated BOMs. Full implementation of the proposed solution is expected to reduce by a 79.50% in the total amount of actual material variance. Moreover, a minimum annual net savings of Php10.5 Million was computed with a net present value of Php42.88 Million in 5 years.
format text
author Li, Lindsey Darlene
Sy, Giza Eileene U.
author_facet Li, Lindsey Darlene
Sy, Giza Eileene U.
author_sort Li, Lindsey Darlene
title A Systems study on the manufacturing system of Unilever Philippines' personal care plant
title_short A Systems study on the manufacturing system of Unilever Philippines' personal care plant
title_full A Systems study on the manufacturing system of Unilever Philippines' personal care plant
title_fullStr A Systems study on the manufacturing system of Unilever Philippines' personal care plant
title_full_unstemmed A Systems study on the manufacturing system of Unilever Philippines' personal care plant
title_sort systems study on the manufacturing system of unilever philippines' personal care plant
publisher Animo Repository
publishDate 2006
url https://animorepository.dlsu.edu.ph/etd_bachelors/9397
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