A system study on the operations department of Manila glass plant

The Manila Glass Plant is a subsidiary of the San Miguel Packaging Products division, which is in charge of producing high quality packaging product for the San Miguel Corporation. The Manila Glass Plant also dominates 70% of the total industry sales, which explains why it is considered as the numbe...

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Main Author: Tan, Michelle
Format: text
Language:English
Published: Animo Repository 1998
Online Access:https://animorepository.dlsu.edu.ph/etd_bachelors/1652
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Institution: De La Salle University
Language: English
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spelling oai:animorepository.dlsu.edu.ph:etd_bachelors-26522021-05-30T06:57:08Z A system study on the operations department of Manila glass plant Tan, Michelle The Manila Glass Plant is a subsidiary of the San Miguel Packaging Products division, which is in charge of producing high quality packaging product for the San Miguel Corporation. The Manila Glass Plant also dominates 70% of the total industry sales, which explains why it is considered as the number one manufacturer of glass containers in the Philippines. The group limited it's study to the procedures being done in the Operations Department's Glass Forming Division, because this is where the heart of manufacturing bottles occur. The main problem of the plant is the During the year 1997, there is deviation of 2.21% metric tons loss reducing the production output by 5,662,092 bottles. This problem proved to be initiated by the insufficient number of teams to perform the Job Change procedure, which resulted to waiting time. The group, through the use of an ARENA 3.0 simulation study, modeled the system to ensure that the results will represent the different alternatives enumerated by the group. An evaluation of alternatives was done in order to determine the best alternative, which is to add another shift to perform the Job Change procedure from 3:00 p.m. to 11:00 p.m. to support the only Job Change shift working from 7:00 a.m. to 3:00 p.m. Through results gathered from the simulation study, the production output of bottles increased beyond expectation of approximately 30% when implementing the proposed system. It minimized the metric tons loss resulting to an increase in the production output, such that, the target output of the company should be 114,991,327 bottles, which is 125% of the total output in 1997. An eight-week program schedule was also arranged for the effective implementation of the proposed system. 1998-01-01T08:00:00Z text https://animorepository.dlsu.edu.ph/etd_bachelors/1652 Bachelor's Theses English Animo Repository
institution De La Salle University
building De La Salle University Library
continent Asia
country Philippines
Philippines
content_provider De La Salle University Library
collection DLSU Institutional Repository
language English
description The Manila Glass Plant is a subsidiary of the San Miguel Packaging Products division, which is in charge of producing high quality packaging product for the San Miguel Corporation. The Manila Glass Plant also dominates 70% of the total industry sales, which explains why it is considered as the number one manufacturer of glass containers in the Philippines. The group limited it's study to the procedures being done in the Operations Department's Glass Forming Division, because this is where the heart of manufacturing bottles occur. The main problem of the plant is the During the year 1997, there is deviation of 2.21% metric tons loss reducing the production output by 5,662,092 bottles. This problem proved to be initiated by the insufficient number of teams to perform the Job Change procedure, which resulted to waiting time. The group, through the use of an ARENA 3.0 simulation study, modeled the system to ensure that the results will represent the different alternatives enumerated by the group. An evaluation of alternatives was done in order to determine the best alternative, which is to add another shift to perform the Job Change procedure from 3:00 p.m. to 11:00 p.m. to support the only Job Change shift working from 7:00 a.m. to 3:00 p.m. Through results gathered from the simulation study, the production output of bottles increased beyond expectation of approximately 30% when implementing the proposed system. It minimized the metric tons loss resulting to an increase in the production output, such that, the target output of the company should be 114,991,327 bottles, which is 125% of the total output in 1997. An eight-week program schedule was also arranged for the effective implementation of the proposed system.
format text
author Tan, Michelle
spellingShingle Tan, Michelle
A system study on the operations department of Manila glass plant
author_facet Tan, Michelle
author_sort Tan, Michelle
title A system study on the operations department of Manila glass plant
title_short A system study on the operations department of Manila glass plant
title_full A system study on the operations department of Manila glass plant
title_fullStr A system study on the operations department of Manila glass plant
title_full_unstemmed A system study on the operations department of Manila glass plant
title_sort system study on the operations department of manila glass plant
publisher Animo Repository
publishDate 1998
url https://animorepository.dlsu.edu.ph/etd_bachelors/1652
_version_ 1772834581895970816