A system study on the liquids and gels and emulsion section of filling and packing department of the Splash Corporation

Splash Corporation has grown from being a backyard business in 1985 to a world class and competitive company. In its 23 years in the industry it has provided quality products and has given employment to our fellow Filipinos. It is currently the largest Filipino-owned company that competes strongly i...

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Main Author: Riofrio, Jofel-Jorrel B.
Format: text
Language:English
Published: Animo Repository 2008
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Online Access:https://animorepository.dlsu.edu.ph/etd_bachelors/2298
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Institution: De La Salle University
Language: English
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spelling oai:animorepository.dlsu.edu.ph:etd_bachelors-32982021-10-21T06:39:11Z A system study on the liquids and gels and emulsion section of filling and packing department of the Splash Corporation Riofrio, Jofel-Jorrel B. Splash Corporation has grown from being a backyard business in 1985 to a world class and competitive company. In its 23 years in the industry it has provided quality products and has given employment to our fellow Filipinos. It is currently the largest Filipino-owned company that competes strongly in an industry that has long been dominated by big multinational corporations. But even with its competitive state, the filing and packing department of Splash Corporation has consistently exceeded its Cycle Time Index(CTI) target of 1.05 from June 2006-July 2007 which resulted to opportunity loss of Php2,411,139.87. With the use of a Fish Bone diagram and Pareto Analysis tool, the problem areas have been identified by the proponent. The root causes identified were Machine Breakdown, Machine Clogging, Meeting during production runs, and Changeover Errors. These problems comprise 87.51% of the total causes of delays that increased the actual cycle time. The delays, in turn, have increased the CTI by 38.24% of its allowable 1.05. After problem analysis and Pareto validation, alternative solutions were made to address the different problem area. The solutions are Early Detection Program (EDP) for machine breakdown, a Pre-measured Adjustment Guide (PMAG) for machine clogging, Weekly Meetings (WM) for meeting problem, Visual Marking of Tube (VMT) for change over delays. The EDP was able to decrease the lost time incurred during machine breakdowns by 86.06% and the PMAG was able to decrease the lost time incurred during machine clogging by 71.30%. The WM and the VMT was able to decrease the lost time incurred by meeting delays and changeover delays by 68.42% and 62.12% respectively. With these solutions, the CTI was reduced by 55.14%. The proponent has showed that the CTI target of 1.05 is only attainable but also manageable to be lowered if the solutions will be continued. The total cost of that has been incurred during the June 2006 to July 2007 that covered labor cost and overhead cost had a total of Php 15,374,570.54. If the solution were used during the same time period the total cost could have only been Php 6,897,723.59. With the cost-benefit analysis done, the comparison between the total investment costs of Php 102,704.00 against the annual benefits of Php 8,476,846.95 resulted to a savings of Php 8,356,142.95. 2008-01-01T08:00:00Z text https://animorepository.dlsu.edu.ph/etd_bachelors/2298 Bachelor's Theses English Animo Repository Cosmetics industry Manufacturing processes Production planning Production control Packaging Engineering
institution De La Salle University
building De La Salle University Library
continent Asia
country Philippines
Philippines
content_provider De La Salle University Library
collection DLSU Institutional Repository
language English
topic Cosmetics industry
Manufacturing processes
Production planning
Production control
Packaging
Engineering
spellingShingle Cosmetics industry
Manufacturing processes
Production planning
Production control
Packaging
Engineering
Riofrio, Jofel-Jorrel B.
A system study on the liquids and gels and emulsion section of filling and packing department of the Splash Corporation
description Splash Corporation has grown from being a backyard business in 1985 to a world class and competitive company. In its 23 years in the industry it has provided quality products and has given employment to our fellow Filipinos. It is currently the largest Filipino-owned company that competes strongly in an industry that has long been dominated by big multinational corporations. But even with its competitive state, the filing and packing department of Splash Corporation has consistently exceeded its Cycle Time Index(CTI) target of 1.05 from June 2006-July 2007 which resulted to opportunity loss of Php2,411,139.87. With the use of a Fish Bone diagram and Pareto Analysis tool, the problem areas have been identified by the proponent. The root causes identified were Machine Breakdown, Machine Clogging, Meeting during production runs, and Changeover Errors. These problems comprise 87.51% of the total causes of delays that increased the actual cycle time. The delays, in turn, have increased the CTI by 38.24% of its allowable 1.05. After problem analysis and Pareto validation, alternative solutions were made to address the different problem area. The solutions are Early Detection Program (EDP) for machine breakdown, a Pre-measured Adjustment Guide (PMAG) for machine clogging, Weekly Meetings (WM) for meeting problem, Visual Marking of Tube (VMT) for change over delays. The EDP was able to decrease the lost time incurred during machine breakdowns by 86.06% and the PMAG was able to decrease the lost time incurred during machine clogging by 71.30%. The WM and the VMT was able to decrease the lost time incurred by meeting delays and changeover delays by 68.42% and 62.12% respectively. With these solutions, the CTI was reduced by 55.14%. The proponent has showed that the CTI target of 1.05 is only attainable but also manageable to be lowered if the solutions will be continued. The total cost of that has been incurred during the June 2006 to July 2007 that covered labor cost and overhead cost had a total of Php 15,374,570.54. If the solution were used during the same time period the total cost could have only been Php 6,897,723.59. With the cost-benefit analysis done, the comparison between the total investment costs of Php 102,704.00 against the annual benefits of Php 8,476,846.95 resulted to a savings of Php 8,356,142.95.
format text
author Riofrio, Jofel-Jorrel B.
author_facet Riofrio, Jofel-Jorrel B.
author_sort Riofrio, Jofel-Jorrel B.
title A system study on the liquids and gels and emulsion section of filling and packing department of the Splash Corporation
title_short A system study on the liquids and gels and emulsion section of filling and packing department of the Splash Corporation
title_full A system study on the liquids and gels and emulsion section of filling and packing department of the Splash Corporation
title_fullStr A system study on the liquids and gels and emulsion section of filling and packing department of the Splash Corporation
title_full_unstemmed A system study on the liquids and gels and emulsion section of filling and packing department of the Splash Corporation
title_sort system study on the liquids and gels and emulsion section of filling and packing department of the splash corporation
publisher Animo Repository
publishDate 2008
url https://animorepository.dlsu.edu.ph/etd_bachelors/2298
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