A system study on the shearing and rollforming facility of Mindanao Steel Corporation

Mindanao Steel Corporation is a manufacturer of quality pre-painted galvanized iron roofing materials and steel roofing accessories. It was established in 1973 in the province of Misamis Oriental in Mindanao. The company is under the F. Jacinto Group Inc., one of the largest business conglomerates i...

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Main Authors: Anzures, Jacqueline, Javier, Oliver Rhey, Reyes, Juan Carlos
Format: text
Language:English
Published: Animo Repository 1997
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Online Access:https://animorepository.dlsu.edu.ph/etd_bachelors/9181
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Institution: De La Salle University
Language: English
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spelling oai:animorepository.dlsu.edu.ph:etd_bachelors-98262021-08-26T07:05:37Z A system study on the shearing and rollforming facility of Mindanao Steel Corporation Anzures, Jacqueline Javier, Oliver Rhey Reyes, Juan Carlos Mindanao Steel Corporation is a manufacturer of quality pre-painted galvanized iron roofing materials and steel roofing accessories. It was established in 1973 in the province of Misamis Oriental in Mindanao. The company is under the F. Jacinto Group Inc., one of the largest business conglomerates in the Philippines. The group performed a system study on MSC and tackled only the shearing and rollforming department found at Novaliches, Quezon City. After weeks of observations, interviews and data collection, the group came up with concerns regarding the production process of the three machines namely the Automatic, Australian and Kawasho through the use of the WOT-SURG Analysis. In pinpointing the direct causes and effects of the problem the group used the Cause and Effect Diagram or Ishikawa Diagram. The problem reached by this step was under-utilization of the three machines. Instead of a 100% machine utilization the company experiences only an 80.53% average machine utilization. After further analysis the true causes that contributes to the problem on machine downtime are: the feeding of coil to uncoiler, transportation of piled cutsheets ad machine repairs. Such move led to choose purchasing of 3 new double coil uncoiler and a new overhead crane as well as the implementation of a preventive maintenance program as best solutions to the problem. The effectiveness of the proposed system was verified through the simulation program on the production process. Basic parameters, considered were the number of orders that arrived, set-up time, total operating time and net operating time. Such parameters were based on the data provided of incoming orders and the time study conducted. The simulation run of the proposed system was 300 working days for 30 repetitions. Results showed that average utilization of each machine is increased to 94.64% for Automatic, 99.11% for Australian and 94.60% for Kawasho respectively. The implementation of the proposed system incurs costs and benefits for the company. The total cost of the proposal to the company, in terms of initial investment, is computed to be P 1,201,500.00. The yearly costs of sustaining the proposal is P 145,191.06. With the proposed system, the quantitative benefits were computed totalled P 359,415.18. The company will receives a total Net Present Value of P 114,811.16 for the whole ten year duration Implementation plan includes: first, presenting the study to the top management then to the executive board of the F. Jacinto Group, second, purchasing of three double coil uncoilers, OH crane and the performance of the preventive maintenance program. It was concluded that the proposal of the group be implemented for it will help the company to increase machine utilization. 1997-01-01T08:00:00Z text https://animorepository.dlsu.edu.ph/etd_bachelors/9181 Bachelor's Theses English Animo Repository System analysis Production management Industrial engineering Steel industry and trade Engineering
institution De La Salle University
building De La Salle University Library
continent Asia
country Philippines
Philippines
content_provider De La Salle University Library
collection DLSU Institutional Repository
language English
topic System analysis
Production management
Industrial engineering
Steel industry and trade
Engineering
spellingShingle System analysis
Production management
Industrial engineering
Steel industry and trade
Engineering
Anzures, Jacqueline
Javier, Oliver Rhey
Reyes, Juan Carlos
A system study on the shearing and rollforming facility of Mindanao Steel Corporation
description Mindanao Steel Corporation is a manufacturer of quality pre-painted galvanized iron roofing materials and steel roofing accessories. It was established in 1973 in the province of Misamis Oriental in Mindanao. The company is under the F. Jacinto Group Inc., one of the largest business conglomerates in the Philippines. The group performed a system study on MSC and tackled only the shearing and rollforming department found at Novaliches, Quezon City. After weeks of observations, interviews and data collection, the group came up with concerns regarding the production process of the three machines namely the Automatic, Australian and Kawasho through the use of the WOT-SURG Analysis. In pinpointing the direct causes and effects of the problem the group used the Cause and Effect Diagram or Ishikawa Diagram. The problem reached by this step was under-utilization of the three machines. Instead of a 100% machine utilization the company experiences only an 80.53% average machine utilization. After further analysis the true causes that contributes to the problem on machine downtime are: the feeding of coil to uncoiler, transportation of piled cutsheets ad machine repairs. Such move led to choose purchasing of 3 new double coil uncoiler and a new overhead crane as well as the implementation of a preventive maintenance program as best solutions to the problem. The effectiveness of the proposed system was verified through the simulation program on the production process. Basic parameters, considered were the number of orders that arrived, set-up time, total operating time and net operating time. Such parameters were based on the data provided of incoming orders and the time study conducted. The simulation run of the proposed system was 300 working days for 30 repetitions. Results showed that average utilization of each machine is increased to 94.64% for Automatic, 99.11% for Australian and 94.60% for Kawasho respectively. The implementation of the proposed system incurs costs and benefits for the company. The total cost of the proposal to the company, in terms of initial investment, is computed to be P 1,201,500.00. The yearly costs of sustaining the proposal is P 145,191.06. With the proposed system, the quantitative benefits were computed totalled P 359,415.18. The company will receives a total Net Present Value of P 114,811.16 for the whole ten year duration Implementation plan includes: first, presenting the study to the top management then to the executive board of the F. Jacinto Group, second, purchasing of three double coil uncoilers, OH crane and the performance of the preventive maintenance program. It was concluded that the proposal of the group be implemented for it will help the company to increase machine utilization.
format text
author Anzures, Jacqueline
Javier, Oliver Rhey
Reyes, Juan Carlos
author_facet Anzures, Jacqueline
Javier, Oliver Rhey
Reyes, Juan Carlos
author_sort Anzures, Jacqueline
title A system study on the shearing and rollforming facility of Mindanao Steel Corporation
title_short A system study on the shearing and rollforming facility of Mindanao Steel Corporation
title_full A system study on the shearing and rollforming facility of Mindanao Steel Corporation
title_fullStr A system study on the shearing and rollforming facility of Mindanao Steel Corporation
title_full_unstemmed A system study on the shearing and rollforming facility of Mindanao Steel Corporation
title_sort system study on the shearing and rollforming facility of mindanao steel corporation
publisher Animo Repository
publishDate 1997
url https://animorepository.dlsu.edu.ph/etd_bachelors/9181
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