CASE STUDY OF INPIT DUMP INSTABILITY AT PIT M PT XYZ

PT XYZ is a coal company located in Tapin, South Kalimantan. One of the active pit of PT XYZ, Pit M, is used as an inpit dump. The in-pit dump which is located in the southern part of Pit M is suffering a failure. Based on the site investigation, failure is still occuring and the in-pit dump materia...

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Main Author: LUTFIAH (NIM : 12114093), IFFAH
Format: Final Project
Language:Indonesia
Online Access:https://digilib.itb.ac.id/gdl/view/27918
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Institution: Institut Teknologi Bandung
Language: Indonesia
id id-itb.:27918
spelling id-itb.:279182018-10-01T14:37:21ZCASE STUDY OF INPIT DUMP INSTABILITY AT PIT M PT XYZ LUTFIAH (NIM : 12114093), IFFAH Indonesia Final Project INSTITUT TEKNOLOGI BANDUNG https://digilib.itb.ac.id/gdl/view/27918 PT XYZ is a coal company located in Tapin, South Kalimantan. One of the active pit of PT XYZ, Pit M, is used as an inpit dump. The in-pit dump which is located in the southern part of Pit M is suffering a failure. Based on the site investigation, failure is still occuring and the in-pit dump material is still moving. To anticipate a bigger movement, a stabilization method is needed to handle the failure so the backfilling activity can be safely continued. <br /> <br /> The stability analysis is carried out with the limit equilibrium method using Slide 6.0 on 2 vertical cross sections along Pit M. The result of the analysis, for both vertical section H and vertical section I, show that different shape of failure are occured. Failure in vertical section H occurs above the embankment of the insitu material so that redesign slope can be done to handle the failure. While, the failure in vertical section I occurs at the end foot of the slope so the best stabilization method is creating the counterweight. <br /> <br /> Redesign of dumping material slope above the material embankment can be carried out with the slope angle of 25o, height of 4.4 m, and bench of 20 m width. While the counterweight design can be carried out with the slope angle 18o and height of 7.9 m. These stabilization methods will give safety factor for vertical section H and I 1.43 and 3.79 respectively. Therefore, the backfilling activity can be continued in Pit M with slope angle 18o, height of 8.4 m, and bench of 60 m width. This design will give safety factor 1.36. text
institution Institut Teknologi Bandung
building Institut Teknologi Bandung Library
continent Asia
country Indonesia
Indonesia
content_provider Institut Teknologi Bandung
collection Digital ITB
language Indonesia
description PT XYZ is a coal company located in Tapin, South Kalimantan. One of the active pit of PT XYZ, Pit M, is used as an inpit dump. The in-pit dump which is located in the southern part of Pit M is suffering a failure. Based on the site investigation, failure is still occuring and the in-pit dump material is still moving. To anticipate a bigger movement, a stabilization method is needed to handle the failure so the backfilling activity can be safely continued. <br /> <br /> The stability analysis is carried out with the limit equilibrium method using Slide 6.0 on 2 vertical cross sections along Pit M. The result of the analysis, for both vertical section H and vertical section I, show that different shape of failure are occured. Failure in vertical section H occurs above the embankment of the insitu material so that redesign slope can be done to handle the failure. While, the failure in vertical section I occurs at the end foot of the slope so the best stabilization method is creating the counterweight. <br /> <br /> Redesign of dumping material slope above the material embankment can be carried out with the slope angle of 25o, height of 4.4 m, and bench of 20 m width. While the counterweight design can be carried out with the slope angle 18o and height of 7.9 m. These stabilization methods will give safety factor for vertical section H and I 1.43 and 3.79 respectively. Therefore, the backfilling activity can be continued in Pit M with slope angle 18o, height of 8.4 m, and bench of 60 m width. This design will give safety factor 1.36.
format Final Project
author LUTFIAH (NIM : 12114093), IFFAH
spellingShingle LUTFIAH (NIM : 12114093), IFFAH
CASE STUDY OF INPIT DUMP INSTABILITY AT PIT M PT XYZ
author_facet LUTFIAH (NIM : 12114093), IFFAH
author_sort LUTFIAH (NIM : 12114093), IFFAH
title CASE STUDY OF INPIT DUMP INSTABILITY AT PIT M PT XYZ
title_short CASE STUDY OF INPIT DUMP INSTABILITY AT PIT M PT XYZ
title_full CASE STUDY OF INPIT DUMP INSTABILITY AT PIT M PT XYZ
title_fullStr CASE STUDY OF INPIT DUMP INSTABILITY AT PIT M PT XYZ
title_full_unstemmed CASE STUDY OF INPIT DUMP INSTABILITY AT PIT M PT XYZ
title_sort case study of inpit dump instability at pit m pt xyz
url https://digilib.itb.ac.id/gdl/view/27918
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