Investigation of 115 kV capacitor bank failure during switching in Chiang Mai 3 substation
In this contribution, the investigation on the failures of 115-kV capacitor banks during switching in Chiang Mai 3 substation is presented. The switching transient is caused by energizing an isolated bank and back-to-back switching. Close time of circuit breaker for energizing capacitor bank, system...
Saved in:
Main Authors: | Kanitpanyacharoen S., Premrudeepreechacharn S. |
---|---|
Format: | Conference Proceeding |
Published: |
2017
|
Online Access: | https://www.scopus.com/inward/record.uri?partnerID=HzOxMe3b&scp=80053653451&origin=inward http://cmuir.cmu.ac.th/jspui/handle/6653943832/42980 |
Tags: |
Add Tag
No Tags, Be the first to tag this record!
|
Institution: | Chiang Mai University |
Similar Items
-
Investigation of 115 kV capacitor bank failure during switching in Chiang Mai 3 substation
by: Sarawut Kanitpanyacharoen, et al.
Published: (2018) -
Studies of lightning overvoltages of 115 kV CMU GIS substation
by: T. Thanasaksiri
Published: (2018) -
Studies of lightning overvoltages of 115 kV CMU GIS substation
by: Thanasaksiri T.
Published: (2017) -
Methods of improving the lightning performance of 22 kV circuit underbuilt on 115 kV transmission lines
by: Thanaphong Thanasaksiri
Published: (2018) -
Study the electrical design of a 22kV substation
by: Mu, Lin
Published: (2016)