PERANCANGAN LINTAS PERAKITAN OVERHEAD LINE DENGAN PENDEKATAN LEAN MANUFACTURING DALAM PROSES PRODUKSI BMW X1 (F48) DI PT GAYA MOTOR

In 2017, BMW Group Indonesia (BGI) announced the highest achievement by a massive <br /> <br /> increase of BMW sales. In the first quarter of 2018, there was also an increase in BMW sales <br /> <br /> compared to the same period in 2017. Of these two achievements, the BMW X...

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Main Author: APRILIANO YOSANDI NIM 13414059, YASSER
Format: Final Project
Language:Indonesia
Online Access:https://digilib.itb.ac.id/gdl/view/31712
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Institution: Institut Teknologi Bandung
Language: Indonesia
id id-itb.:31712
spelling id-itb.:317122018-09-07T09:56:55ZPERANCANGAN LINTAS PERAKITAN OVERHEAD LINE DENGAN PENDEKATAN LEAN MANUFACTURING DALAM PROSES PRODUKSI BMW X1 (F48) DI PT GAYA MOTOR APRILIANO YOSANDI NIM 13414059, YASSER Indonesia Final Project INSTITUT TEKNOLOGI BANDUNG https://digilib.itb.ac.id/gdl/view/31712 In 2017, BMW Group Indonesia (BGI) announced the highest achievement by a massive <br /> <br /> increase of BMW sales. In the first quarter of 2018, there was also an increase in BMW sales <br /> <br /> compared to the same period in 2017. Of these two achievements, the BMW X1 is the main <br /> <br /> product that has the biggest sales increase so that BGI predicts an increase in demand for BMW <br /> <br /> X1 in the future. <br /> <br /> This successful attainment was achieved by BGI by cooperating with PT Gaya Motor, a <br /> <br /> company who engaged in the assembly of four-wheeled vehicles, such as BMW, with the <br /> <br /> production process based completely knocked down. To anticipate the increasing demand, the <br /> <br /> company evaluates one common takt time method which is no longer relevant and results in a <br /> <br /> low productivity assembly line, especially in the overhead line. <br /> <br /> Low productivity was solved through the newly proposed assembly line design using the lean <br /> <br /> manufacturing approach, such as waste elimination, line balancing using ranked positional <br /> <br /> weight and largest candidate rule method, process activity mapping, workgroup process <br /> <br /> mapping, layout evaluation using spaghetti diagrams, and 5S. <br /> <br /> It is known that excess motion is the highest type of waste with a proportion of 43.50%. The <br /> <br /> solution provided was proven to increase productivity by decreasing idle time by 1545.74 <br /> <br /> seconds and smoothness index by 850.73, increasing line efficiency by 15.30% and production <br /> <br /> capacity from 12 to 16 units per day, as well as a more optimal layout proposal. text
institution Institut Teknologi Bandung
building Institut Teknologi Bandung Library
continent Asia
country Indonesia
Indonesia
content_provider Institut Teknologi Bandung
collection Digital ITB
language Indonesia
description In 2017, BMW Group Indonesia (BGI) announced the highest achievement by a massive <br /> <br /> increase of BMW sales. In the first quarter of 2018, there was also an increase in BMW sales <br /> <br /> compared to the same period in 2017. Of these two achievements, the BMW X1 is the main <br /> <br /> product that has the biggest sales increase so that BGI predicts an increase in demand for BMW <br /> <br /> X1 in the future. <br /> <br /> This successful attainment was achieved by BGI by cooperating with PT Gaya Motor, a <br /> <br /> company who engaged in the assembly of four-wheeled vehicles, such as BMW, with the <br /> <br /> production process based completely knocked down. To anticipate the increasing demand, the <br /> <br /> company evaluates one common takt time method which is no longer relevant and results in a <br /> <br /> low productivity assembly line, especially in the overhead line. <br /> <br /> Low productivity was solved through the newly proposed assembly line design using the lean <br /> <br /> manufacturing approach, such as waste elimination, line balancing using ranked positional <br /> <br /> weight and largest candidate rule method, process activity mapping, workgroup process <br /> <br /> mapping, layout evaluation using spaghetti diagrams, and 5S. <br /> <br /> It is known that excess motion is the highest type of waste with a proportion of 43.50%. The <br /> <br /> solution provided was proven to increase productivity by decreasing idle time by 1545.74 <br /> <br /> seconds and smoothness index by 850.73, increasing line efficiency by 15.30% and production <br /> <br /> capacity from 12 to 16 units per day, as well as a more optimal layout proposal.
format Final Project
author APRILIANO YOSANDI NIM 13414059, YASSER
spellingShingle APRILIANO YOSANDI NIM 13414059, YASSER
PERANCANGAN LINTAS PERAKITAN OVERHEAD LINE DENGAN PENDEKATAN LEAN MANUFACTURING DALAM PROSES PRODUKSI BMW X1 (F48) DI PT GAYA MOTOR
author_facet APRILIANO YOSANDI NIM 13414059, YASSER
author_sort APRILIANO YOSANDI NIM 13414059, YASSER
title PERANCANGAN LINTAS PERAKITAN OVERHEAD LINE DENGAN PENDEKATAN LEAN MANUFACTURING DALAM PROSES PRODUKSI BMW X1 (F48) DI PT GAYA MOTOR
title_short PERANCANGAN LINTAS PERAKITAN OVERHEAD LINE DENGAN PENDEKATAN LEAN MANUFACTURING DALAM PROSES PRODUKSI BMW X1 (F48) DI PT GAYA MOTOR
title_full PERANCANGAN LINTAS PERAKITAN OVERHEAD LINE DENGAN PENDEKATAN LEAN MANUFACTURING DALAM PROSES PRODUKSI BMW X1 (F48) DI PT GAYA MOTOR
title_fullStr PERANCANGAN LINTAS PERAKITAN OVERHEAD LINE DENGAN PENDEKATAN LEAN MANUFACTURING DALAM PROSES PRODUKSI BMW X1 (F48) DI PT GAYA MOTOR
title_full_unstemmed PERANCANGAN LINTAS PERAKITAN OVERHEAD LINE DENGAN PENDEKATAN LEAN MANUFACTURING DALAM PROSES PRODUKSI BMW X1 (F48) DI PT GAYA MOTOR
title_sort perancangan lintas perakitan overhead line dengan pendekatan lean manufacturing dalam proses produksi bmw x1 (f48) di pt gaya motor
url https://digilib.itb.ac.id/gdl/view/31712
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