Investigation of 115 kV capacitor bank failure during switching in Chiang Mai 3 substation

In this contribution, the investigation on the failures of 115-kV capacitor banks during switching in Chiang Mai 3 substation is presented. The switching transient is caused by energizing an isolated bank and back-to-back switching. Close time of circuit breaker for energizing capacitor bank, system...

وصف كامل

محفوظ في:
التفاصيل البيبلوغرافية
المؤلفون الرئيسيون: Sarawut Kanitpanyacharoen, Suttichai Premrudeepreechacharn
التنسيق: وقائع المؤتمر
منشور في: 2018
الموضوعات:
الوصول للمادة أونلاين:https://www.scopus.com/inward/record.uri?partnerID=HzOxMe3b&scp=80053653451&origin=inward
http://cmuir.cmu.ac.th/jspui/handle/6653943832/49915
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المؤسسة: Chiang Mai University
الوصف
الملخص:In this contribution, the investigation on the failures of 115-kV capacitor banks during switching in Chiang Mai 3 substation is presented. The switching transient is caused by energizing an isolated bank and back-to-back switching. Close time of circuit breaker for energizing capacitor bank, system loads, and power factors are varied in the simulations by PSCAD/EMTDC program to determine the causes of maximum inrush current and overvoltage. Simulation results of energizing isolated bank suggest that the maximum inrush currents occurs with a higher system load while the maximum overvoltage occurs in a lower system load. The back-to-back switching sequence of capacitor banks has given different results. Method No.1 is the most optimal sequence for energizing capacitor bank and is most likely to minimize the effects of back-to-back switching. © 2011 IEEE.