ENERGY EFFICIENCY IMPROVEMENT IN GEOTHERMAL POWER PLANT WITH THE APPLICATION OF LOAD-BASED GAS REMOVAL SYSTEM AND COOLING WATER PUMP CONTROL SYSTEM

From a thermodynamic perspective, the operation of a Geothermal Power Plant (GPP) follows the Rankine cycle. Efficient electricity generation is achieved through the conservation of energy (enthalpy) of steam from the well to the generator, setting low condensation pressure to achieve maximum ene...

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Main Author: Wibisono
Format: Theses
Language:Indonesia
Online Access:https://digilib.itb.ac.id/gdl/view/46423
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Institution: Institut Teknologi Bandung
Language: Indonesia
id id-itb.:46423
spelling id-itb.:464232020-03-05T08:41:40ZENERGY EFFICIENCY IMPROVEMENT IN GEOTHERMAL POWER PLANT WITH THE APPLICATION OF LOAD-BASED GAS REMOVAL SYSTEM AND COOLING WATER PUMP CONTROL SYSTEM Wibisono Indonesia Theses geothermal power plant, ejector technology, gas removal system optimization, ejector simulation, ejector control system, cooling system optimization INSTITUT TEKNOLOGI BANDUNG https://digilib.itb.ac.id/gdl/view/46423 From a thermodynamic perspective, the operation of a Geothermal Power Plant (GPP) follows the Rankine cycle. Efficient electricity generation is achieved through the conservation of energy (enthalpy) of steam from the well to the generator, setting low condensation pressure to achieve maximum energy conversion in the turbine, and minimal electricity consumption (house-load). In almost all GPPs, condensation (condenser) pressure is maintained by the vacuum ejector, which absorbs the accumulation of Non-Condensable Gas (NCG), namely CO2 and H2S. Condensation effectiveness relies heavily on the availability of cooling water, which depends on the performance of the cooling water circulation pump. In general, GPPs are designed to work on base-load (100% capacity); therefore, the performance of supporting equipment such as ejectors and pumps is not sensitive to fluctuations in generation loads or changes in NCG content (percent weight in total steam supply). This insensitiveness results in almost constant houseload and ejector's motive steam consumptions. In the operation of GPP X, the NCG content is only 35% of its design, while the daily generation fluctuates below the base-load according to grid regulator instructions. This dynamic operation provides an opportunity for energy efficiency efforts through modification of the ejector system and cooling circulation pump to be more adaptive to changes in load, which ultimately supports conservation of steam reserves. Performance analysis and design of control systems for ejectors and circulating cooling water pumps are the scopes of the thesis discussion that performs option evaluation, which includes: regulating cooling water rate, controlling motive steam flow, or the combination of both, and also physical modification of the ejector. text
institution Institut Teknologi Bandung
building Institut Teknologi Bandung Library
continent Asia
country Indonesia
Indonesia
content_provider Institut Teknologi Bandung
collection Digital ITB
language Indonesia
description From a thermodynamic perspective, the operation of a Geothermal Power Plant (GPP) follows the Rankine cycle. Efficient electricity generation is achieved through the conservation of energy (enthalpy) of steam from the well to the generator, setting low condensation pressure to achieve maximum energy conversion in the turbine, and minimal electricity consumption (house-load). In almost all GPPs, condensation (condenser) pressure is maintained by the vacuum ejector, which absorbs the accumulation of Non-Condensable Gas (NCG), namely CO2 and H2S. Condensation effectiveness relies heavily on the availability of cooling water, which depends on the performance of the cooling water circulation pump. In general, GPPs are designed to work on base-load (100% capacity); therefore, the performance of supporting equipment such as ejectors and pumps is not sensitive to fluctuations in generation loads or changes in NCG content (percent weight in total steam supply). This insensitiveness results in almost constant houseload and ejector's motive steam consumptions. In the operation of GPP X, the NCG content is only 35% of its design, while the daily generation fluctuates below the base-load according to grid regulator instructions. This dynamic operation provides an opportunity for energy efficiency efforts through modification of the ejector system and cooling circulation pump to be more adaptive to changes in load, which ultimately supports conservation of steam reserves. Performance analysis and design of control systems for ejectors and circulating cooling water pumps are the scopes of the thesis discussion that performs option evaluation, which includes: regulating cooling water rate, controlling motive steam flow, or the combination of both, and also physical modification of the ejector.
format Theses
author Wibisono
spellingShingle Wibisono
ENERGY EFFICIENCY IMPROVEMENT IN GEOTHERMAL POWER PLANT WITH THE APPLICATION OF LOAD-BASED GAS REMOVAL SYSTEM AND COOLING WATER PUMP CONTROL SYSTEM
author_facet Wibisono
author_sort Wibisono
title ENERGY EFFICIENCY IMPROVEMENT IN GEOTHERMAL POWER PLANT WITH THE APPLICATION OF LOAD-BASED GAS REMOVAL SYSTEM AND COOLING WATER PUMP CONTROL SYSTEM
title_short ENERGY EFFICIENCY IMPROVEMENT IN GEOTHERMAL POWER PLANT WITH THE APPLICATION OF LOAD-BASED GAS REMOVAL SYSTEM AND COOLING WATER PUMP CONTROL SYSTEM
title_full ENERGY EFFICIENCY IMPROVEMENT IN GEOTHERMAL POWER PLANT WITH THE APPLICATION OF LOAD-BASED GAS REMOVAL SYSTEM AND COOLING WATER PUMP CONTROL SYSTEM
title_fullStr ENERGY EFFICIENCY IMPROVEMENT IN GEOTHERMAL POWER PLANT WITH THE APPLICATION OF LOAD-BASED GAS REMOVAL SYSTEM AND COOLING WATER PUMP CONTROL SYSTEM
title_full_unstemmed ENERGY EFFICIENCY IMPROVEMENT IN GEOTHERMAL POWER PLANT WITH THE APPLICATION OF LOAD-BASED GAS REMOVAL SYSTEM AND COOLING WATER PUMP CONTROL SYSTEM
title_sort energy efficiency improvement in geothermal power plant with the application of load-based gas removal system and cooling water pump control system
url https://digilib.itb.ac.id/gdl/view/46423
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